.
We began with a pleasant breakfast at Stiftsgarden with
meusli and fil followed by bacon and egg with a little herring as a side dish.
Kristin was coughing badly at breakfast but is sufficiently
improved to have washed the boat and removed stains from the whole above water
hull. ~We then tried to apply a waterline stripe but failed utterly to get it
to stick down smoothly in the place we wanted it to be. The result was
frustration and we abandoned the idea.
In the mean time I’d been working on the under kitchen
Blakes seacock which had stuck. It’s almost impossible to get at the locknuts
keeping the securing bolts tight but I did get there in a very uncomfortable
position and a curse or two.
I then sampled the fuel tank finding a little water and some
rather cloudy fuel at the bottom but less than half a litre so I’ll just add
more anti bug treatment. The prefilter looks fine. The use of FAME in diesel
fuel makes this problem endemic nowadays. Another routine job was to change the gearbox
lubricant which would have been easier with the boat upside down. I’m no longer
happy to work doubled up. There’s too much of me in the way.
I did more work on the mast and had a tug at the aerial lead
wire finding it surprisingly easy to move. Now the yard had damaged the aerial
making it pretty ineffective a year ago so I needed to fit a new aerial but had
been frightened of the risks of changing the aerial lead up the mast. It is
very easy to break the cable or the auxiliary string.
Anyway, finding the lead movable I cut the old lead off at
the base of the mast, spliced it to a piece of thin cordage and pulled the old
cable out of the top of the mast followed by all the spare cordage as Alan
Burwin had once told me so as to have a remedy later in case of accident. I
then attached the new aerial lead to the cordage and started pulling it down
the mast. This proved difficult. The problem was excessive friction at the top
of the mast caused by bending the new lead on entry. It proved beneficial to
prefeed the new cable in through the hole at the top of the mast. Even so it
was hard work and became impossible when I started to pull the old cable back
down the mast with the new one. The extra cordage length was insufficient. I
cut off the cordage and resumed pulling only to find the new lead was fouled on
other cables inside the mast at the exit hole. I managed to clear this by the
high tech method of prodding with a pair of scissors and the aerial lead then
emerged. We then had to push and feed the next 15 metres of cable through the
mast to get the full length needed to reach the VHF radio. We were very
relieved to get that far. In addition Totta has accepted my plea for a later
launch on Friday so we can have breakfast at the hotel and leave in time to
attend the launch at 9:30 a.m.
We are having a rest now and then going out for
more Suchi for supper.
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